Preliminary Field Evaluation of Mercury Control Using Combustion Modifications | |
Lissianski, V. ; Maly, P. ; Marquez, T. | |
GE Energy and Environmental Research Corporation | |
关键词: Removal; Modifications; Combustion; Testing; 01 Coal, Lignite, And Peat; | |
DOI : 10.2172/938958 RP-ID : None RP-ID : FC26-03NT41725 RP-ID : 938958 |
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美国|英语 | |
来源: UNT Digital Library | |
【 摘 要 】
In this project EER conducted a preliminary field evaluation of the integrated approach for mercury (Hg) and NO{sub x} control. The approach enhanced the 'naturally occurring' Hg capture by fly ash through combustion optimization, increasing carbon in ash content, and lowering ESP temperature. The evaluation took place in Green Station Units 1 and 2 located near Henderson, Kentucky and operated by Western Kentucky Energy. Units 1 and 2 are equipped with cold-side ESPs and wet scrubbers. Green Station Units 1 and 2 typically fire two types of fuel: a bituminous coal and a blend of bituminous coals based on availability. Testing of Hg emissions in Unit 2 without reburning system in operation and at minimum OFA demonstrated that efficiencies of Hg reduction downstream of the ESP were 30-40%. Testing also demonstrated that OFA system operation at 22% air resulted in 10% incremental increase in Hg removal efficiency at the ESP outlet. About 80% of Hg in flue gas at ESP outlet was present in the oxidized form. Testing of Hg emissions under reburning conditions showed that Hg emissions decreased with LOI increase and ESP temperature decrease. Testing demonstrated that maximum Hg reduction downstream of ESP was 40-45% at ESP temperatures higher than 300 F and 60-80% at ESP temperatures lower than 300 F. The program objective to demonstrate 80% Hg removal at the ESP outlet has been met.
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938958.pdf | 746KB | download |