5th International Conference on Manufacturing, Optimization, Industrial and Material Engineering | |
Car Assembly Line Efficiency Improvement by Lean Principle | |
Sawassalung, Suwalee^1 ; Chutima, Parames^1,2 | |
Industrial Engineering Department, Chulalongkorn University, Bangkok | |
10330, Thailand^1 | |
Regional Centre for Manufacturing Systems Engineering, Chulalongkorn University, Bangkok | |
10330, Thailand^2 | |
关键词: Assembly line; Car manufacturers; Design standard; Lean principles; Manpower costs; Production cost; Value stream mapping; Waste analysis; | |
Others : https://iopscience.iop.org/article/10.1088/1757-899X/215/1/012009/pdf DOI : 10.1088/1757-899X/215/1/012009 |
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来源: IOP | |
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【 摘 要 】
This research aimed to increase the efficiency of actual working time to compare to design standard time ratio (DSTR) as per analysing process of Lean System of the assembly line in a car manufacturer in Thailand. Currently, the case study factory and its group of factories, which have many branches all over the world, have competed with each other on quality, delivered time and production cost. The production cost which can reduce without affecting quality and acceptable by clients is the manpower cost. The index of competition is DSTR. The factory now has DSTR of 6.13 and DSTR of the assembly department is 4.24 which is very high comparing to other departments. The low DSTR indicates that the factory has good quality. The ways to solve the problem are to apply the following tools, i.e. Lean principle, Value Stream Mapping (VSM), Waste Analysis and ECRS. After implementing the above tools, the results showed that DSTR decreased from 4.24 to 4.06 or 4.25%.
【 预 览 】
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Car Assembly Line Efficiency Improvement by Lean Principle | 939KB | ![]() |