ACHIEVING NEW SOURCE PERFORMANCE STANDARDS (NSPS) EMISSION STANDARDS THROUGH INTEGRATION OF LOW-NOx BURNERS WITH AN OPTIMIZATION PLAN FOR BOILER COMBUSTION | |
Penrod, Wayne ; Moyeda, David | |
Sunflower Electric Power Corporation (United States) | |
关键词: Modifications; Boilers; Testing; Burners; Air; | |
DOI : 10.2172/827045 RP-ID : NONE RP-ID : FC26-03NT41418 RP-ID : 827045 |
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美国|英语 | |
来源: UNT Digital Library | |
【 摘 要 】
The objective of this project is to demonstrate the use of an Integrated Combustion Optimization System to achieve NO{sub x} emissions levels in the range of 0.15 to 0.22 lb/MMBtu while simultaneously enabling increased power output. The project consists of the integration of low-NO{sub x} burners and advanced overfire air technology with various process measurement and control devices on the Holcomb Station Unit 1 boiler. The project includes the use of sophisticated neural networks or other artificial intelligence technologies and complex software that can optimize several operating parameters, including NO{sub x} emissions, boiler efficiency, and CO emissions. The program is being performed in three phases. In Phase I, the boiler is being equipped with sensors that can be used to monitor furnace conditions and coal flow to permit improvements in boiler operation. In Phase II, the boiler will be equipped with burner modifications designed to reduce NO{sub x} emissions and automated coal flow dampers to permit on-line fuel balancing. In Phase III, the boiler will be equipped with an overfire air system to permit deep reductions in NO{sub x} emissions to be achieved. Integration of the overfire air system with the improvements made in Phases I and II will permit optimization of the boiler performance, output, and emissions. During this reporting period, efforts were focused on Phase I and Phase II activities. The furnace sensors were procured and installed in February 2003. Baseline testing was performed following the sensor installation. The low-NO{sub x} burner modifications, the coal flow dampers, and the coal flow monitoring system were procured and installed during a boiler outage in March 2003. Process design activities were performed to support design of the equipment installed and to develop specifications for the overfire air system. The overfire air system preliminary engineering design was initiated.
【 预 览 】
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827045.pdf | 200KB | download |