IMPROVED MISCIBLE NITROGEN FLOOD PERFORMANCE UTILIZING ADVANCED RESERVOIR CHARACTERIZATION AND HORIZONTAL LATERALS IN A CLASS I RESERVOIR--EAST BINGER (MARCHAND) UNIT | |
Sinner, Joe | |
Binger Operations (United States) | |
关键词: Oil Wells; 02 Petroleum; Reservoir Engineering; Directional Drilling; Site Characterization; | |
DOI : 10.2172/824381 RP-ID : NONE RP-ID : FC26-00BC15121 RP-ID : 824381 |
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美国|英语 | |
来源: UNT Digital Library | |
【 摘 要 】
Implementation of the work program of Budget Period 2 of the East Binger Unit (''EBU'') DOE Project continues. The drilling of new horizontal well EBU 63-2H, scheduled for this reporting period, was delayed due to a lack of rig availability. This well was spud near the end of the reporting period. EBU 59-1 was converted to injection service, and injection capacity at the plant was increased from 19 MMscf/d to 22 MMscf/d. Although other factors have temporarily limited the field's ability to fully utilize the increased capacity, injection in the pilot area has been increased over 2 MMscf/d since the start of the project. Nitrogen recycle within the pilot area has been reduced with the projects implemented to date. Prior to pilot development, nitrogen production was 56% of nitrogen injected. Currently, nitrogen production is only 26% of injection. Pilot area oil production has increased 90 bpd or 30%, with 160 bpd from new wells offset by a loss of 70 bpd from wells converted to injection.
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