科技报告详细信息
IMPROVED MISCIBLE NITROGEN FLOOD PERFORMANCE UTILIZING ADVANCED RESERVOIR CHARACTERIZATION AND HORIZONTAL LATERALS IN A CLASS I RESERVOIR--EAST BINGER (MARCHAND) UNIT
Sinner, Joe
Binger Operations (United States)
关键词: Oil Wells;    02 Petroleum;    Reservoir Engineering;    Directional Drilling;    Site Characterization;   
DOI  :  10.2172/824381
RP-ID  :  NONE
RP-ID  :  FC26-00BC15121
RP-ID  :  824381
美国|英语
来源: UNT Digital Library
PDF
【 摘 要 】

Implementation of the work program of Budget Period 2 of the East Binger Unit (''EBU'') DOE Project continues. The drilling of new horizontal well EBU 63-2H, scheduled for this reporting period, was delayed due to a lack of rig availability. This well was spud near the end of the reporting period. EBU 59-1 was converted to injection service, and injection capacity at the plant was increased from 19 MMscf/d to 22 MMscf/d. Although other factors have temporarily limited the field's ability to fully utilize the increased capacity, injection in the pilot area has been increased over 2 MMscf/d since the start of the project. Nitrogen recycle within the pilot area has been reduced with the projects implemented to date. Prior to pilot development, nitrogen production was 56% of nitrogen injected. Currently, nitrogen production is only 26% of injection. Pilot area oil production has increased 90 bpd or 30%, with 160 bpd from new wells offset by a loss of 70 bpd from wells converted to injection.

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