Topical Report ''Corrosion Evaluation of LLW2 Skid-B Weld Failure Mechanisms (44139-92) | |
Chang, JI Young | |
United States. West Valley Demonstration Project Act. | |
关键词: Pipelines; 36 Materials Science; 12 Management Of Radioactive Wastes, And Non-Radioactive Wastes From Nuclear Facilities; Llw2; Failure; | |
DOI : 10.2172/782734 RP-ID : 44139-92 RP-ID : AC24-81NE44139 RP-ID : 782734 |
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美国|英语 | |
来源: UNT Digital Library | |
【 摘 要 】
An independent investigation of pipe welding leaks from the Low-Level Waste 2 (LLW2) Skid-B System for the possibilities of improper welding (IW), microbiologically influenced corrosion (MIC), sensitization, chloride pitting corrosion (CPC), and intergranular stress corrosion cracking (IGSCC) was conducted. The results show the prevailing mechanisms that caused the leaks are identified as IW, CPC, and the improper selection of weld filler material for the base metals in an environment of the North Plateau underground water. These is no evidence of MIC, sensitization, or IGSCC. The chloride pitting corrosion mechanism that took place at all the welds are also described. All the pipelines were replaced with polyvinyl chloride (PVC) for cost saving and the LLW2 Skid B System has been successfully operating since 1999. This report summarizes the findings and recommendations associated with preventive measures for future operations. The LLW2 Facility is a replacement for an existing waste treatment system. The Facility processes two different waste streams through two different ''skids.'' After seven months of operation, one of the two skids began to leak. Extensive evaluation of the corrosion mechanisms and the contributing factors are documented in this report. This report principally evaluates the physical and chemical configurations that led to the corrosion and leaks. Chloride pitting corrosion, exacerbated by weld defects, is the corrosion mechanism. The report also discusses fabrication and Quality Assurance (QA)/Quality Control (QC) actions that would have prevented their occurrence. It is believed that in the absence of either the defects or the chloride concentrations, corrosion would not have occurred. In developing the specification for processing skids to be used in the Facility, high chloride was not identified as a parameter of concern. As such, piping fabrication and inspection standards for the system did not identify more rigorous welding standards that could have prevented the corrosion and subsequent leaks.
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