A Method to Increase Current Density in a Mono Element Internal Tin Processed Superconductor Utilizing Zr Oxide to Refine Grain Size | |
Bruce A. Zeitlin, Eric Gregory | |
关键词: CURRENT DENSITY; EXTRUSION; FABRICATION; GEOMETRY; GRAIN SIZE; HARDNESS; HEAT TREATMENTS; OXIDES; OXYGEN; REFINING; SUPERCONDUCTORS; VELOCITY Superconductivity; Nb3Sn; Materials; Accelerator Magnets; | |
DOI : 10.2172/926654 RP-ID : Final Report Phase 2 PID : OSTI ID: 926654 Others : TRN: US1204485 |
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美国|英语 | |
来源: SciTech Connect | |
【 摘 要 】
The effect of Oxygen on (Nb1Zr)3Sn multifilament conductors manufactured by the Mono Element Internal Tin (MEIT) process was explored to improve the current density by refining the grain size. This followed work first done by General Electric on the Nb3Sn tape process. Techniques to fabricate the more difficult Nb1Zr composites are described and allowed fabrication of long lengths of .254 mm diameter wire from an 88.9 mm diameter billet. Oxygen was incorporated through the use of SnO2 mixed with tin powder and incorporated into the core. These were compared to samples with Ti+Sn and Cu+Sn cores. Heat treatments covered the range of 700 C to 1000 C. Current density vs. H, grain size, and reaction percentages are provided for the materials tested. The Oxygen gave superior results in the temperature range of 815-1000 C. It also stabilized the filament geometry of the array in comparison to the other additions at the higher temperatures. At 815 C a peak in layer Jc yielded values of 2537 A/mm2 at 12 T and 1353 A/mm2 at 15T, 8-22% and 30-73% greater respectively than 700 C values. Results with Oxygen at high temperature show the possibility of high speed continuous reaction of the composite versus the current batch or react in place methods. In general the Ti additions gave superior results at the lower reaction temperature. Future work is suggested to determine if the 815 C reaction temperature can lead to higher current density in high tin (Nb1Zr+Ox)3Sn conductors. A second technique incorporated oxygen directly into the Nb1Zr rods through heat treatment with Nb2O5 at 1100 C for 100 hours in vacuum prior to extrusion. The majority of the filaments reduced properly in the composite but some local variations in hardness led to breakage at smaller diameters.
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