Analysis of failed and nickel-coated 3093 beam clamp components at the East Tennessee Technology Park (ETTP). | |
Singh, D. ; Pappacena, K. ; Gaviria, J. ; Burtsteva, T. ; Nuclear Engineering Division | |
关键词: ALUMINIUM; CHEMICAL ANALYSIS; CORROSION; CORROSION PRODUCTS; ELECTROCHEMICAL CORROSION; GASEOUS DIFFUSION; HARDNESS; HYDROGEN; HYDROGEN EMBRITTLEMENT; MICROSCOPY; NICKEL; ROCKWELL HARDNESS; SAMPLE PREPARATION; STAINLESS; | |
DOI : 10.2172/993696 RP-ID : ANL-10/19 PID : OSTI ID: 993696 Others : TRN: US201024%%111 |
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美国|英语 | |
来源: SciTech Connect | |
【 摘 要 】
The U.S. Department of Energy and its contractor, Bechtel Jacobs Company (BJC), are undertaking a major effort to clean up the former gaseous diffusion facility (K-25) located in Oak Ridge, TN. The decontamination and decommissioning activities require systematic removal of contaminated equipment and machinery followed by demolition of the buildings. As part of the cleanup activities, a beam clamp, used for horizontal life lines (HLLs) for fall protection, was discovered to be fractured during routine inspection. The beam clamp (yoke and D-ring) was a component in the HLL system purchased from Reliance Industries LLC. Specifically, the U-shaped stainless steel yoke of the beam clamp failed in a brittle mode at under less than 10% of the rated design capacity of 14,500 lb. The beam clamp had been in service for approximately 16 months. Bechtel Jacobs approached Argonne National Laboratory to assist in identifying the root cause of the failure of the beam clamp. The objectives of this study were to (1) review the prior reports and documents on the subject, (2) understand the possible failure mechanism(s) that resulted in the failed beam clamp components, (3) recommend approaches to mitigate the failure mechanism(s), and (4) evaluate the modified beam clamp assemblies. Energy dispersive x-ray analysis and chemical analysis of the corrosion products on the failed yoke and white residue on an in-service yoke indicated the presence of zinc, sulfur, and calcium. Analysis of rainwater in the complex, as conducted by BJC, indicated the presence of sulfur and calcium. It was concluded that, as a result of galvanic corrosion, zinc from the galvanized components of the beam clamp assembly (D-ring) migrated to the corroded region in the presence of the rainwater. Under mechanical stress, the corrosion process would have accelerated, resulting in the catastrophic failure of the yoke. As suggested by Bechtel Jacobs personnel, hydrogen embrittlement as a consequence of corrosion was also explored as a failure mechanism. Corroded and failed yoke samples had hydrogen concentrations of 20-60 ppm. However, the hydrogen content reduced to 4-11 ppm (similar to baseline as-received yoke samples) when the corrosion products were polished off. The hydrogen content in the scraped off corrosion product powders was >7000 ppm. These results indicate that hydrogen is primarily present in the corrosion products and not in the underlying steel. Rockwell hardness values on the corroded yoke and D-rings were R{sub c} {approx} 41-46. It was recommended to the beam clamp manufacturer that the beam clamp components be annealed to reduce the hardness values so that they are less susceptible to brittle failure. Upon annealing, hardness values of the beam clamp components reduced to R{sub c} {approx} 25. Several strategies were recommended and put in place to mitigate failure of the beam clamp components: (a) maintain hardness levels of both yokes and D-rings at R{sub c} < 35, (b) coat the yoke and D-rings with a dual coating of nickel (with 10% phosphorus) to delay corrosion and aluminum to prevent galvanic corrosion since it is more anodic to zinc, and (c) optimize coating thicknesses for nickel and aluminum while maintaining the physical integrity of the coatings. Evaluation of the Al- and Ni-coated yoke and D-ring specimens indicated they appear to have met the recommendations. Average hardness values of the dual-coated yokes were R{sub c} {approx} 25-35. Hardness values of dual-coated D-ring were R{sub c} {approx} 32. Measured average coating thicknesses for the aluminum and nickel coatings for yoke samples were 22 {micro}m (0.9 mils) and 80 {micro}m (3 mils), respectively. The D-rings also showed similar coating thicknesses. Microscopic examination showed that the aluminum coating was well bonded to the underlying nickel coating. Some observed damage was believed to be an artifact of the cutting-and-polishing steps during sample preparation for microscopy.
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